1:27'.93n 103:16'.36e
Wednesday 20th October
Anchorage near
Malacca
Captain’s Log:
0700hrs left the marina -quite misty and headed for the
bridge then skirted around the top of the ship anchorage and headed for the
southern tip of the Malaysian peninsular.
Pleased to say alternator
working like a treat. Ran generator to make water - so we now have full
batteries, full fuel tank and full water tank - life is good. Very bad
visibility in all the humidity - very little wind. Spent a lot of time
dodging fishing nets slung between small fishing boats
This is the oil or gas depot we passed close to
Malacca
Endless rows
of these fishing stakes(withies) block the inshore path
So we have to
mix up with the ships in their lane instead!
and rows of withie, which seem to run from the
shore out for about 4 miles to the inshore low water mark.
The alternator seems to be working as it should which
is a relief so could afford to run the extractor fan for the engine room, it
draws 18 amps so have not been able to use it before. This turned out
to be a mixed blessing as it was removing the smell of boiling batteries!!!
It transpired that George's idea of by-passing the blocking diode was not a
good one - so rewired it as before when we got to the anchorage; we will see
if that works.
The smoke
haze from woods being burnt in nearby Sumatra!
Position 1:27'.93n 103:16'.36e
Distance run 40.1 miles average speed 6.5 knots.
0700hrs left in heavy mist after a night full of
thunder and lightning but little rain.
Spent most of the day keeping in the shallows to dodge
the worst of the tide and avoiding fishing nets, tide finally turned in our
favour at 1300hrs. Went down for a siesta came on deck at 1500 to find
engine overheating
1 Shut it down and started to beat to windward with a
light wind dead on the nose! Pulled out a spare raw water pump and
started to change the pump - not easy with a red hot engine, shut the water
off and as I did that the main water elbow into the water inlet manifold
cracked and water started pouring into the boat! Shut off main seacock in a
bit of a hurry, so now had two jobs pump on the engine and the water
inlet. Changed the pump by 1800hrs and repaired the elbow with epoxy -
this lasted for about 5 minutes and opened up again also new water pump
leaking - stupid me had not changed the gaskets! At least we could use the
engine for the last couple of miles into the anchorage. Worked until
23.00 hrs getting everything fixed. I hope! At least the batteries seem
fine today.
Position 2:06'.51n 102:20.52e
Distance run 75 miles
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